So it's been a while since I've updated this thread, and catch everything back up to date.
After May last year, and the "starting fluid episode" I was in need of an new intercooler.
As I mentioned previously, I decided to ditch the thinner Saab unit (with plastic endtanks) and upgrade to a full metal intercooler. I didn't necessarily have the coin to drop on a more efficient unit, so I got the tried/true ebay IC and started in on making it "work."

after a little loving w/ my die grinder and a jig saw, we were starting to get somewhere:


Being that this was a 2.5" thick core vs the 1.5" core I had previously, things were a bit tighter on the engine side than before...

Once I got my measurements, I knew how wide I could go with the entire unit, and I started to fab up new end tanks:


Little more cutting, little more trimming, little more fitting:

and all tacked together w/ my spool gun for my MIG welder:


FWIW, while in theory it'll work great, welding AL with a spool gun is def not an easy feat. I'm sure with a lot more practice I could make prettier/more functional welds, but man... what a pain!
This is about as good of a weld as I could do when practicing, and it's for this reason that I found someone w/ a TIG welder to finish up everything! I didn't want my IC to look like complete shicahcah!

Additionally, I wasn't able to get enough heat into the weld that it was giving me full penetration, so I feared that it would blow apart eventually under constant abuse.
After coming back from the first TIG welder, this was the initial setup:

As I mentioned before, this IC is a fair bit bigger than my original, and I didn't really design my bumpers, core support, etc to support a bigger IC... so things were TIGHT
His welds were a LOT prettier than mine, btw

Once I got the IC roughed in place, I went to adding mounts to my core support to fasten everything down:


and then after a trip to another TIG welder (this one was closer than the last, hence 2 different welders) to weld on one more pipe and to finish up the bottom pipe for my BOV, it was time to make everything pretty with a little wrinkle coating!

This was my first time using this stuff, and it actually came out fairly nicely FWIW...

and everything installed back in the car:

Things were tight for sure, but the car survived 2 track events and a fair bit of miles and experienced no contact what-so-ever. So that was a relief at least.
The next thing that was up to upgrade was the radiator as well. On the really hot track days, my coolant temps would get a bit higher than I liked, and I generally needed to run the heater in the car (insult to injury) to keep everything under control. In order to combat this, I was able to get a custom radiator built (for a fair bit cheaper than the Ron Davis ones 034 sells):


As you can see, this one is a fair bit thicker than the OEM, giving me a bit mroe capacity, etc. Only downside to this one over the 034 radiator is that I had to add threaded inserts for the fan shroud mounts, etc. Not the end of the world, and very worth the savings IMHO, but one downside.
And with the nice shiny new radiator, I of course needed to clean up the shroud that was weathered and slightly rusty:



and with some trimming and adjusting, everything popped right into place (including my custom side shrouds to the radiator)


At this point, the 'ol girl made it to three track events. It made its track debue at Watkins Glen II in August. The tune was far from ideal, but she ran. Car was loud as anything w/ the temporary summit point $25 resonator welded onto the exhaust (to the point I needed earplugs on the way up/back), but it made it there w/o a hitch!
Unfortunately, life at the track wasn't too great b/c teh improved design 034 trigger wheel failed on the second run of the day, leaving me with 5 of 6 screws sheered off.

Thankfully, sun does shine on a dog's a$$ every now and again, and I was able to find a full on machine shop in Watkins Glen with CNC machines and the whole 9 yards. After talking with the owner for a bit and acting truly pathetic and hopeless, he put aside what he was doing and helped me drill and retap the holes. Additionally, there was a hardware store in town that stocked 3mm screws as well... I struck gold for sure.

Needless to say, this is not the site people are used to in the paddock garages:

I had it apart at 4pm on Monday, and had it back together first thing Tuesday morning in time for the first instructor session... so I was over the moon excited to get the 'ol girl back on track again.
Unfortunately the event didn't end w/o issues, as the rear seal on the center diff let go and started spraying transmission fluid all over my exhaust. It was at that point we tossed in the towel and I swapped spots with my dad's car and ended up towing the 'ol girl home...

we had a bleeder!

but after some time under the car (having Wiley's old 016 trans w/ high bias center diff in my garage) and with Wiley's help, we were able to toss the new center diff on my transmission and get it all buttoned up. From there, I was able to take the 'ol bird out for two more events, one in Summit Point and one at VIR. Car performed well. I really need to tune it properly and get more boost thrown in, but for now she's happy with her younger siblings


I think this pretty much catches me up to date. Have some things to do over the winter to finish buttoning up the car (namely powdercoating trim, finish installing interior, fix WG bolts that backed out, etc), but hopefully I can get out in March for what may be my last event for a while, as the family is about to grow by one!